Now comes this, the National Transportation Safety Board is preparing to release a report that places blame on a ground crew in Syracuse that didn't report a FOOT LONG GASH in a plane that IT HAD PUT THERE when someone DROVE A TRUCK INTO THE PLANE during boarding. The plane took off and just minutes later ripped open and depressurized resulting in it making an emergency landing in Buffalo.
During nwa's bankrupcty proceedings, the company replaced Northwest employees at 60 stations across the network, replacing them with outsourced employees. The outsourced employees have no connection to nwa other than they work the flights. They are employees or a separate company and are compensated at much lower rates than previously. This saves nwa loads of money but has always had questionable side effects. We have been hearing stories of numerous problems with the outsourced companies (AirWisconsin, the company involved in this incident, is a very well respected company and this incident is an abberation for them) but now we have had two incidents in the last month that has cost one life and nearly cost 100 more here.
Remember people, cheap doesn't always equate to bargain. There are always reasons why something is cheaper. Something has been cut out someplace.
Below is the article...taken from WEAN 10 website in Syracuse
Flight 1411 was en route from Syracuse to Detroit when just 20 minutes into the flight, decompression occurred. Oxygen masks dropped, and the plane was headed toward an emergency landing in Buffalo. On the ground, an inspection showed a 12-inch gash had opened in the fuselage.
An NTSB preliminary report, due to be released in a few days, is
The episode is virtually identical to an incident two years ago in Seattle. An Air Alaska jet was forced to return for an emergency landing after a decompression episode caused by a 12-inch gash found in the fuselage. A ground crew member had struck the plane with his loading cart but failed to report it because he said the damage did not seem severe.
In the case of that Air Alaska incident, a ground crew member was suspended, while other members had to undergo safety training. At this point, there's no word what, if any, disciplinary action is planned for the ground crew in Syracuse.
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